12-02-2005, 06:25 PM | #1 |
Rock Crawler Join Date: Sep 2005 Location: wyckoff, NJ
Posts: 639
| what am i doing wrong?
Please dont flame me, i'm new to electric stuff and am trying to figure out what i'm doin wrong. i have a maxx based crawler with an evx stock motorwith gd600 and hitec 5955 and hitec 5998. i am using a 7 cell battery. now when crawling everything is fine until i use the rear steer and turn the front when i do this i lose throttl. what causes this to happen? is it to much for the speed controler ? what can i do to fix this? please help cause i'm tired of throwing my radio at my crawler. thanks
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12-02-2005, 06:31 PM | #2 |
06 Super National Champ Join Date: Jun 2004 Location: Stark Industries Bar and Grill
Posts: 11,361
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The EVX doesn't have enough BEC current capabilities to handle 4WS. You need to run a RX pack. |
12-02-2005, 06:31 PM | #3 |
2006 2.2 National Champ Join Date: Dec 2004 Location: Big Bear Lake
Posts: 8,328
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The EVX's BEC can't handle the 2 high torque servos and the throttle at the same time. It can be fixed two ways..... 1. Run an RX pack to power the servos. 2. Buy an ESC that has a higher BEC rating, like a used Super Rooster or a Tekin Rebel 2. |
12-02-2005, 06:45 PM | #4 |
Colt Python/SR9c Join Date: Feb 2004 Location: out in the shop, reloading ammo!
Posts: 8,626
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running and RX pack doesn't always work with the evx either.. you will sometimes still get the glitching
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12-02-2005, 06:58 PM | #5 |
Rock Crawler Join Date: Sep 2005 Location: wyckoff, NJ
Posts: 639
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well i just put an rx in there and it seems to work fine but i will have to do some crawlin before i know for sure. thanks for your help
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